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Date: Mon, 19 Jan 1998 11:49:36 -0600
From: Ron Price <RPRICE@wp*.it*.lu*.ed*>
To: jeff_h@pi*.co*
Cc: techdiver@aquanaut.com
Subject: Divers Supply Press Release -Reply
Jeff,
Thanks for your post.  I have a couple of questions
after reading your post.

1)  Was gas turn based on 1/3s or some other
calculation?

2) I assume Mike had his own lift bag.  You don't say in
your post, but did Mike deploy his lift bag for ascent? 
The post makes it sound as if all were using Andre's
line for ascent.  I ask, because if everyone was using
Andre's, and Mike still had his lift bag - why would
 would try to drag his down.  Just use Mike's to
provide the needed lift?

I ask only to try to learn from this tragic event.  
Thanks,
Ron

>>> Jeff Hirschman <jeff_h@pi*.co*> 01/18/98
09:56am >>>
For the people who would like to know the real truth....
Here it is....  And
I'm sorry if the facts don't agree with the fantasies of
others.



Official Press Release
of
Divers Supply
Compiled by: Jeff Hirschman, Dick McNatt, Renee
LaChapelle,
Larry Roth, and Captain Ed Cooke

January 18, 1997

This report was compiled from all the known facts as it
pertains to the
accident which
occurred on January 12, 1998 that involved Andre B.
Smith, John S. Claypool,
and Mike
J. Elkins.  There is no speculation or exaggeration in
this report.  Only
the facts as known
to us will be conferred in this report.

Dive team consisted of:
Andre B. Smith, 57	over 10,300+ logged dives.  35+
years experience in
military, 
			commercial, sport, and technical 
diving.  Instructor trainer who was 
			qualified to teach novice through
the top levels of technical diving.

John S. Claypool, 34	Experienced in sport, technical,
and law enforcement
diving.  
			Instructor qualified to teach
novice through advanced nitrox.

Mike J. Elkins, 36	Experienced in sport and
technical diving, pursuing
further training 
			in order to improve his skills and
capabilities.

Larry J. Roth, 42	Experienced in military, sport,
and technical diving.
			29+ years experience.

Dive Plan:
This was to be the second trimix dive in Elkins class. 
The plan called for
a dive on a sandy
bottom to a depth of 250 fsw (feet sea water)with a
bottom time of 20
minutes - gas supply
permitting.  All divers were configured with a trimix
consisting of 17%
Oxygen, 38%
Helium, and 45% Nitrogen which was contained in twin
low pressure steel 95
cubic foot
tanks with an isolation manifold system.  The travel
gas, a 40% Nitrox (40%
Oxygen, 60%
Nitrogen) mix was contained in a single low pressure
72 or 80 cubic foot
scuba tank
mounted on the left side of the divers harness.  The
decompression gas, a
80% Nitrox
(80% oxygen, 20% Nitrogen) mix was contained in a
single low pressure 72 or
80 cubic
foot scuba tank and was mounted on the right side of
the divers harness.
Additionally, two
72 cubic foot decompression bottles (Nitrox 80%) and
one 72 cubic foot
travel gas (Nitrox
40%) were ready aboard the vessel if needed.  All
equipment and redundant
configurations
were in compliance with IANTD (International
Association Nitrox and
Technical Divers)
standards.

 
Dive Profile:
The decompression schedule was planned for
*100fsw/1min  90fsw/1min  80fsw/1min
70fsw/3min  60fsw/2min  50fsw/5min  40fsw/6min 
**30fsw/8min  20fsw/13min
10fsw/28min		Backup plan (if Nitrox-80 lost)
30fsw/10min  20fsw/19  10fsw/45

*Switch to Nitrox 40%			**Switch to
Nitrox 80%  

Eyewitness account of surviving team member:
On 12 January 1998,  I was a member of the dive
team consisting of Andre Smith-
IANTD Trimix Instructor, Mike Elkins- IANTD Technical
Nitrox Certified
Diver, John
Claypool- IANTD Trimix Certified Diver and myself-
IANTD Trimix Certified
Diver. 
The team's goal was to make a discovery dive in the
area of the "Classic
Barges" off the
coast of West Palm Beach, Florida.  Additionally, Mike
Elkins was making the
second
trimix dive of his IANTD Trimix certification program as
Andre's student.
Futaba Elkins
was also aboard as a Technical Nitrox student of
Andre's and our safety
diver.  The boat
used for the dive was the SS Minnow operated by
Captain Ed Cooke.  Due to
the speed
with which events unfolded and the difficulties
experienced, this is my best
recollection of
the entire incident.

A dive plan was worked out by Mike and myself
separately, then compared and
approved,
by Andre.  The plan was for a 250 fsw dive for 20
minutes bottom time, 68
minutes
decompression for a total run time of 99 minutes
surface to surface.  All
diver's gas
consumption rates allowed for safe completion of the
planned dive.  Gases
were planned
for 17/38/45 bottom mix, 40% nitrox travel mix, and
80% decompression mix.
All gases
were mixed and verified in the West Palm Beach
Diver's Supply store by Andre
and each
respective diver .  

Gear preparation was completed aboard the Minnow
without problem, followed
by a dive
briefing.  The brief consisted of the dive plan, surface
and decompression
plan, and
emergency procedures.  Every member of the team
fully understood the plan
and executed
it correctly.

All divers entered the water and descended normally. 
Bottom conditions were
approximately 1/4 kt north current, 60 ft visibility.  A
slow drift dive was
started with all
divers remaining in close proximity.  During this portion
of the dive Mike
was having
difficulty with his buoyancy trim and was kicking
vigorously to stay off the
bottom.  He
appeared to be struggling,  so I went up to him and
encouraged him to add
more air to his
buoyancy compensator, then raised the back of his
tanks to help shift any
trapped air and
improve his trim.  He waved me off and appeared to
relax some.  I stayed
right next to him
and we continued to drift until we stopped a few
moments later to inspect
some concrete
rubble.

At this time Mike signaled to Andre that he was at his
bottom mix turn limit. 
(Approximately 15 minutes into the dive.)  We then
assumed our ascent
positions .  I was
on Andre's right, John on his left and Mike on John's
left.  Andre released
the first liftbag
as planned and we started to ascend.  After rising to
about 200 fsw, we
started to sink and
Mike appeared to be having trouble adding and/or
venting air from his buoyancy
compensator.  Andre assisted Mike and we started to
go up again and rose to
about 175
fsw.  Mike was still experiencing buoyancy problems
and possibly perceived
he was
running out of air.  We started to descend again and
my view was obscured by
all the
bubbles rising up to my face.  Before I could determine
were the air was
coming from, we
descended to about 220 fsw.  Andre handed me the
buoy line to keep it clear
of us while
he devoted his attention to Mike.  The liftbag deflated
sometime during this
descent. 
Andre began to quickly pull it down to use to pull Mike
up.  John,  now too
away far to
assist, had begun his own ascent and I had my first
opportunity to get in
front of Mike to
assist him.  He was beginning to panic and may have
exhausted his bottom
gas.  Before I
could get to him with my octopus,  Mike began
breathing off his travel mix.
Due to the
great depth and high partial pressure of oxygen in the
mixture he was now
breathing, his
"central nervous system oxygen toxicity" level was
dangerously high as was
the chance of
oxygen induced convulsions.  I grabbed Mike by the
tank manifold and inflated my
buoyancy compensator (vest) fully to try and drag both
Mike and Andre to the
100 fsw
level where we could more safely handle the problem. 
We got to
approximately 150 fsw,
when I felt a shudder in my hand.  I was hoping Andre
was shaking Mike
instead of the
onset of his convulsions.  When I looked down Mike
was not moving.  I now
ran out of
air,  stopped swimming and tried to get Andre's
attention for air or to
signal him to meet
me up higher.  Andre may have been trying to share
his own air supply with
Mike, but my
view was blocked.  We had now sunk back down
to180 fsw at which point I lost
my hold
while trying to get around Mike to Andre.  Since my
buoyancy compensator was
fully
inflated I could not stay with them.

While I was trying to control my ascent, I saw John
above me and attempted
to join him. 
He had his liftbag out and was preparing to inflate it.  I
caught up to him
but could not stop
my rate of ascent until 80 fsw.  I looked down and saw
John, he still
appeared fine.  I then
began to descend down to my first decompression
stop at 100 fsw.  While
stabilizing
myself  I lost sight of John.

Since I was now alone, I deployed my liftbag and
began my decompression
schedule while
I tried to determine how best to modify it, in view of the
problems.  I
tried to signal the
boat with my bag while I  looked for the others.  Later I
heard a boat
engine revving at high
RPM.  I hoped the others had surfaced and were
heading for the beach.  After
about 30
minutes a boat drifted up to me and then moved out of
my view.  Later I saw
another boat,
that stayed with me.  It pulled up on top of me and I
then knew it was the
Minnow.  I
finished my new decompression schedule and
surfaced after 125 minutes.

Once onboard, I found none of the other divers
onboard and briefed the
Captain on the
situation.  Captain Cooke  told me that Andre's liftbag
had come up before
mine, but no
one was with it.  There was only about 90 minutes of
daylight left, so I
suggested we
request a USCG helicopter and then helped Captain
Cooke organize a search
pattern to
find the lost divers.  Search conditions were excellent
and the sea state
low.  The Coast
Guard data marker beacons (DMB) were easily visible
on the surface, making the
probability of finding a surfaced diver very high.  We
searched until 0400
the next day,
returning only once to refuel.  USCG assets joined
immediately and searched
through
January 15th and Sheriffs department through January
16th.

 
Conclusion:
A search was attempted on the bottom of the accident
site on Thursday,
January 15th but
was aborted due to weather conditions.  An extensive
search was conducted on
the bottom
of the accident site on Saturday, January 17th.  The
teams consisted of:
1) RV Ocean Window (561) 252-2526
2) Captain Ed Cooke of the SS Minnow with
	Trimix Divers: Jeff Hirschman, Renee
LaChapelle, and Mike Haverstock
	Safety Divers: Major R.T. Keegan, Sergeant G.
Webb, and Officer D. Howard
	2nd Support Team: Larry Roth, Pete Winston,
Douglas Frederick

Results of the surface and bottom searches:
There were no discoveries or recoveries made.
	
We would like to thank the following groups and
individuals for all of their
help in this
tragic event:
	USCG Station Lake Worth
	Helo Golf November
	Captain Bob Johnson of Rampage Dive
Charters
	Palm Beach Sheriffs Department - Dive teams,
boat crews, and air search units
	RV Ocean Window (561) 252-2526
	West Palm Police Department and dive team
	Captain Ed Cooke of SS Minnow
	And all of those who have gone out of their way
to help
--
Jeff Hirschman

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